throbber
WEATHERFORD INTERNATIONAL, LLC, et al.
`
`EXHIBIT 1002
`
`
`
`WEATHERFORD INTERNATIONAL, LLC, et al.
`'
`'
`V.
`
`PACKERS PLUS ENERGY SERVICES, INC.
`
`SPE
`
`Society of‘ Petroleum Engineers
`
`SPE 19090
`
`A
`
`‘
`
`Production and Stimulation Analysis of Multiple
`Hydraulic Fracturing of a 2,000-ft Horizontal Well
`by A.B. Yost ll, U.S. DOE/METC, and W.K. Overbey Jr., BDM Engineering Services Co.
`SPE Membem
`
`This paper was prepared lor presentation at the SPE Gas Technology Symposium held in Dallas, Texas, June 7-9, 1989.
`This paper was selected for presentation by an SPE Program Committee following review of information contained in an abstract submitted by the author(s). Contents of the paper,
`as presented. have not been reviewed by the Society of Petroleum Engineers and are subject to correction by the author(s). The material, as presented. does not necessarily reflect
`any position of the Society of Petroleum Engineers, its officers, or members. Papers presented at SPE meetings are subject to publication review by Editorial Committees of the Society
`of Petroleum Engineers. Permission to copy is restricted to an abstract of not more than 300 words. illustrations may not be copied. The abstract should contain conspicuous acknowledgment
`of where and by whom the paper is presented. Write Publications Manager, SPE, P.O. Box 833836. Richardson, TX 75083-3836. Telex, 730989 SPEDAL.
`
`ABSTRACT
`
`The performance of multiple hydraulic fracturing
`treatments along a 2000-foot horizontal wellbore was
`completed in a gas bearing, naturally—fractured shale
`gas
`reservoir
`in Wayne County, west Virginia.
`Pre-
`frac
`flow and pressure data, hydraulic fracturing
`treatments, and post-stimulation flow and pressure
`data
`form the
`basis
`from which
`a
`comprehensive
`analysis was
`performed.
`Average
`field production
`from 72 wells was
`used
`as baseline data
`for
`the
`analysis.
`Such data was used to show the significance
`of
`enhanced production from a horizontal well
`in
`a field that was partially depleted.
`
`The post-frac stabilized flow rate was '95,D00
`feet
`per
`day
`(mcf/d)
`from 2000
`feet of
`cubic
`horizontal borehole. Under current reservoir pressure
`conditions,
`the horizontal well produced at a
`rate
`7
`times greater
`than the field current average of
`13 mcfd for stimulated vertical wells.
`This increase
`in
`gas production suggests
`that
`-horizontal wells,
`in strategically placed locations within partially
`depleted
`fields,
`could
`significantly
`increase
`reserves .
`
`BACKGROUND
`
`has
`The Federal Government
`investigating
`been
`the application of high angle and horizontal drilling
`in tight
`formations
`for more
`than 20 years.
`The
`value of high angle drilling and multiple hydraulic
`fracturing from an
`inclined or horizontal
`borehplg
`for maximizing production was
`recognized in 1969.
`1
`The first test of the concept was performed by Mobil
`Oil Corporation in the Austin chalk in which a well
`inclined to 6 °
`through the pay zone was stimulated
`three
`times. 2)
`The U.S.
`Bureau
`of Mines,
`in
`cooperation with Columbia Gas and Consolidated Natural
`Gas, drilled inclined wells
`in the Devonian shales
`
`References and illustrations at end of paper.
`
`and again in 1976.00
`of west Virginia in 1972(3)
`These wells obtained inclinations of 43°
`and
`52°
`respectively,
`but
`production
`results were mixed
`and
`not
`convincing
`of
`the
`potential
`for
`the
`technique.
`
`The stimulation aspects of horizontal drilling
`represent
`a
`technical challenge in tight
`formations
`where the horizontal wellbore may not always provide _
`adequate economic production. Little or no published
`literature exists
`on
`the mechanics
`of hydraulic
`fracturing of horizontal wells.
`Typically,
`long
`horizontal wells
`are completed with preperforated
`liners to preserve hole integrity.
`The disadvantage
`of
`this type of completion is the associated risk
`of pulling the liner at a
`later stage of production
`history and re-running and cementing a casing string
`such
`that
`selective
`placement of
`fracturing of
`fluids can be accomplished.
`
`isolation
`zone
`is
`approach
`alternative
`An
`accomplished by the installation of external casing
`packers
`and port collars
`as
`an
`integral part of
`a
`casing string .in the horizontal
`section.
`Such
`a
`completion
`arrangement
`provided
`stimulation
`intervals with ready-made perforations for injecting
`fracturing
`fluids
`in
`an
`open
`hole
`fracturing
`condition
`behind pipe.
`This was
`the method of
`completion used in this 2000 foot horizontal well
`to avoid the problems of formation damage associated
`with
`cementing
`and
`to
`eliminate
`the
`need
`for
`tubing—conveyed perforating of
`numerous
`treatment
`intervals.
`
`to
`designed
`stimulations’ were
`of
`series
`A
`open and propagate the many known natural
`fractures
`that existed along the 2000 foot length of horizontal
`wellbore.
`The
`stimulations were
`also
`designed
`to induce
`fractures
`in the
`formation as well
`as
`propagate natural
`fractures by manipulating pressure
`and injection rates.
`
`oiibf 14
`
`01 of 14
`
`

`
`PRODUCTION AND STIMULATION ANALYSIS OF
`MULTIPLE HYDRAULIC FRACTURING OF A 2000-FOOT HORIZONTAL WELL
`
`SPE 19090
`
`gas-low deviation factor evaluated
`@ initial pressure
`formation temperature, degrees R.
`formation thickness, ft.
`
`247
`=
`(h
`interval
`shale
`the whole
`Assuming
`ft) to be productive and with a formation temperature
`of 93°F, stabilized gas production rate of 35 mcfpd,
`and
`the
`slope
`from the Horner plot of
`15863.2
`psia?/cycle;
`therefore
`formation permeability (K)
`is calculated as follows:
`
`K =
`
`1637)(34)(0.0107)(0.980
`(15863.2)(247)
`
`553
`
`= 0.082 md (2).
`
`permeability
`for
`value
`estimated
`above
`The
`a conventional well
`in a
`similar
`to those of
`is
`low permeability
`reservoir with
`a
`very
`large
`fracture.
`As discussed previously,
`these analyses
`are
`not
`strictly applicable
`to
`the
`horizontal
`wellbore geometry, but one may assume a horizontal
`wellbore to represent
`a vertical well with a
`long,
`finite conductivity fracture.
`
`an
`RET #1.
`for
`test
`Following they build—up
`attempt was made
`to isolate and individually test
`each of the seven zones representing a total
`interval
`of
`2211
`feet
`(3803-6014
`feet).
`A
`combination
`straddle tool was designed to facilitate the opening
`and
`closing of port collars
`in
`seven
`individual
`zones.
`
`test
`pressure_ build-up
`hour
`twenty-four
`A
`_
`followed by a 24-hour drawdown
`for each zone was
`performed using the combination straddle tool.
`In
`order
`to estimate permeability for
`each isolated
`zone,
`a
`three-dimensional,
`dual
`porosity,
`single
`phase ‘gas
`simulator
`reservoir model was used to
`determine permeability values
`shown
`in Table
`1.
`The average preestimulation permeability was 0.0665
`md.
`
`pressure
`the
`of
`analysis
`stimulation
`Post
`determination
`resulted 'in
`build—up/drawdown
`data
`skin values,
`of average reservoir pressure values,
`the various
`and
`average permeability values
`for
`zones with the different stimulation jobs. Results
`of the pressure build—up analysis using the various
`techniques are summarized in Table 2.
`
`were
`techniques
`analysis
`pressure
`Various
`to
`obtain
`estimates
`of
`used
`post-stimulation
`build-up
`data
`permeability.
`Selective
`pressure
`were
`analyzed using type-curve matching, Horner's
`technique,
`and
`a
`newly—developed
`technzgue
`known
`as the Rectangular Hyperbolic Method (RHM)
`:3)-
`
`indicated
`6
`Post-stimulation analysis for Zone
`a post—frac permeability of 0.1835 md, but an average
`- reservoir pressure of 205 psia using history matching
`process.
`Analysis of
`the pressure build—up data
`using Horner's
`technique was not possible due
`to
`the
`fact
`that
`the
`stabilized flow period prior
`to the build-up test was very short, hence accurate
`results
`of
`pressure
`and
`permeability could
`not
`be
`determined.
`Instead,
`type-curve matching was
`implemented
`for
`the analysis
`and an average per-
`meability value was
`calculated to be 0.1795 md.
`Both
`techniques
`indicated similar
`results,
`hence
`more
`confidence was
`generated
`in
`the
`estimated
`post—frac permeability value.
`
`
`INTRODUCTION
`
`of Energy's Morgantown
`The U.S. Department
`contracted with
`the
`BDM
`Energy Technology Center
`Corporation
`to
`select
`a site, drill,
`core,
`log,
`complete,
`test
`and
`stimulate a horizontal well
`in
`the Devonian
`shales.
`The
`area
`selected for
`the
`site was
`in Lincoln District, Wayne County, west
`Virginia,
`as
`shown
`in Figure
`1.
`Upon
`completion
`of drilling operations which were conducted between
`October
`and December,
`1986,
`the
`RET
`#1 well was
`completed,
`as
`shown
`in Figure 2,
`by
`installing 8
`external
`casing packers
`(ECPs)
`as
`an integral part
`of the 4-1/2 inch casing string along with 14 sliding
`sleeve ported collars which were
`used to provide
`access
`to the
`formation
`in lieu of perforations.
`The casing string was not
`cemented
`in place, but
`anchored by one external.casing packer located inside
`the 8-5/8 inch casing.
`A cement packer was
`included
`in the string as
`a backup system in case the ECPs
`failed to inflate; however, 7 of the 8 ECPs pressure
`tested okay,
`and
`thus
`7
`separate open hole
`zones
`were available for testing.
`
`conducted in
`test was
`frac
`4—stage data
`One
`Zone 6 to obtain data on breakdown pressure, closure
`pressure,
`fracture gradient
`and
`stress
`ratio for
`use in designing the primary stimulation test series
`for
`the well.
`Three
`stimulations were
`conducted
`in Zone
`1
`to determine the most suitable fluid and
`injection rate; Ehis
`informati n was
`reported in
`SPE Papers
`17759 5
`and
`18249 5).
`Evaluation of
`the
`first
`three
`fractures
`pointed
`the direction
`for
`design
`and
`implementation .of
`the
`final
`two
`stimulations
`conducted
`on
`the well.
`The
`results
`of
`these
`stimulations
`and
`the performance of
`the
`of all
`stimulations
`is
`the
`well
`upon
`completion
`subject of this paper.
`
`Pre- and Post-Frac well Testing and Analysis
`
`initiated
`testing phase was
`initial well
`The
`with a 640-hour pressure build—up test of the entire
`2160
`feet
`(excluding ECPs) of open—hole behind 14
`port
`collars opposite
`7
`isolated zones.
`Surface
`wellhead
`gauge
`pressure
`and
`orifice meter
`run
`pressures were used to establish reservoir permea-
`bility.
`
`are
`techniques
`analysis
`transient
`Classical
`not strictly applicable to the horizontal wellbore
`geometry, but was used to obtain initial estimates
`of
`reservoir properties
`to be used as
`a starting
`point for the simulation analysis.
`
`rock pressure
`initial/estimated reservoir
`The
`was 192 psia from extrapolation of the_Horner plot.
`It
`is important
`to note that
`the average reservoir
`pressure
`in
`the
`surrounding wells was
`determined
`to be between 188-200 psia based on a 7-day pressure
`build—up test.
`The value of Kh was calculated from
`the following equation:
`
`Kh = 1637 qavg”iZiT
`m
`
`(1)
`
`.
`slope = 15863.2
`average gas production rate, mscfpd
`formation permeability, md
`gas viscosity, Cp evaluated at initial
`pressure, P1
`
`m E
`
`where:
`
`avg "IIIIII
`
`Hi
`
`02 03f"’14
`
`02 of 14
`
`

`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`Albert B. Yost II and William K. Overbey, Jr.
`
`3
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`SPE 19090
`
`
`.303 md, average reservoir pressure
`permeability was
`1 was stimulated by 3 different frac jobs
`Zone
`was 178 psia, and skin factor was >D.00.
`A positive
`at various treating pressures and rates with nitrogen,
`skin
`value was
`calculated for Zones
`5
`and
`8.
`
`liquid C02,
`and nitrogen-foani with proppants. Hell
`A
`indicating a
`slightly damaged well.
`drop
`in
`testing procedures
`and data analysis were performed
`the
`skin factor
`from -2.87 for
`the overall well
`
`
`
`for each job.
`In the first job when the well was
`
`to a more positive value for Zones
`5 and 8 could
`stimulated with N2, pressure build-up data indicated
`
`be attributed to:
`
`
`a
`reservoir pressure of
`290 psia which
`is
`above
`the
`current
`average
`reservoir
`pressure
`(185-200
`
`(a)
`the
`sand
`problem that was
`encountered
`psia
`as
`determined
`by
`the
`7-day
`shut-in
`test).
`during the clean-up process, hence indicating damage
`1
`This
`is due
`to the fact
`that Zone
`(N2 frac) was
`to the wellbore;
`_
`still overpressured by the amount of
`inerts present
`(b)
`the decrease
`in the analyzed horizontal
`in the
`gas mixture at
`the time of
`testing.
`The
`section of
`the wellbore from 2160 feet (all zones)
`simulation of
`the pressure buildup data using G3DFR
`pre-stimulation
`analysis,
`to
`932
`feet
`(Zones
`5
`model
`estimated an
`average permeability equal
`to
`and 8) post-stimulation analysis.
`0.0477 md. Analysis of
`the pressure build-up data
`following the
`second job ( C02
`frac)
`indicated a
`
`
`tested using
`The accuracy of these results was
`permeability value of 0.0480 and 0.0485 using Horner's
`three different
`techniques;.
`Estimating
`values of
`technique and history matching,
`respectively.
`Using
`
`
`
`average reservoir pressure (P)
`RHM
`using
`the
`Horner's technique,
`reservoir pressure was estimated
`
`technique
`has
`an
`advantage over
`the conventional
`at 182 psia. Results of build—up pressure analysis
`
`methods
`because
`knowledge
`of
`neither
`the
`
`
`following
`the
`third
`job
`(N3-foam—proppant
`frac)
`well/reservoir
`configuration
`nor
`the
`boundary
`indicated the presence of
`a
`dual porosity system
`
`
`a
`condition
`is
`required
`for
`routine
`build-up
`with the middle region having a slope one-half that
`
`
`analysis.
`However,
`conventional methods
`such
`as
`of
`the late region on
`the build-up curve which is
`
`Horner's technique, when correctly used, will provide
`characteristic of
`a
`dual
`porosity system in
`the
`superior
`results of
`Kh
`and
`S values
`compared to
`Devonian
`shale.
`The
`average
`permeability
`was
`estimated at
`0.090 md,
`and
`the
`average pressure
`the
`RHM technique.
`Therefore,
`values
`of
`K
`and
`S for Zones
`5 and 8 are believed to be in the range
`was determined to be 184 psia.
`
`of 0.300 md
`to 0.492 md
`and
`-0.881
`to
`1.386,
`
`were
`stimulated
`using
`4
`and
`2-3
`Zones
`respectively, whereas the average reservoir pressure
`is calculated at 178 psia based on the RHM technique.
`period,
`Following
`the
`cleanup
`N2-foam/proppant.
`
`a
`rate of 62 mcfd for
`Zones 2-3 and 4 produced at
`well Stimulation Summary
`a period of
`35 days.
`Pressure build-up analysis
`using Horner's
`technique
`indicated
`an
`average
`reservoir permeability of 0.1505 md
`and an average
`pressure of 182 psia.
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`stimulated using Ng-foam/
`and 8 were
`5
`Zones
`proppant. Analysis‘ of pressure build-up data
`has
`
`
`indicated an average reservoir pressure of 178 psia
`and an average permeability of 0.310 md.
`
`
`
`5 and 8 were
`Pressure build-up data from Zones
`analyzed
`using
`type—curve
`matching,
`Horner's
`
`technique,
`and
`the Rectangular Hyperbolic Method
`
`(RHM).
`Values
`of
`average
`reservoir
`pressure,
`formation
`flow capacity,
`and
`skin
`factor were
`estimated.
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`The objective of stimulation research in the
`horizontal wellbore was
`to determine the recovery
`efficiency of
`the natural
`fracture systenl and the
`effects
`expected
`from hydraulically
`fracturing
`the well whenever multiple
`fractures would
`be
`induced.
`To determine the most effective wellbore
`stimulation under these conditions, it was necessary
`to use a systematic approach to examine the effects
`of
`various
`combinations
`of
`four
`factors, which
`were:
`(1)
`type of fluid (e.g., gas,
`liquid,
`foam);
`(2)
`fluid injection rate;
`(3)
`volume
`of
`fluid
`injected;
`and
`(4)
`bottomhole
`treating
`pressure.
`Following each stimulation,
`flow rate and buildup
`test
`data
`were
`used
`to
`determine
`permeability-thickness
`product
`and
`flow
`rate
`improvement ratio.
`Key stimulation issues identified
`WEN-.‘:I
`
`
`
`to the complexity of production from the
`Due
`Devonian shale and the existence of'a dual porosity
`system,
`a
`log—log plot of AP2
`(P2wsPwf), and d(AP2)
`be
`could
`that
`fractures
`number of
`the
`(1)
`(derivative
`of
`delta
`pressure
`squared)
`versus
`Effective
`Time
`(Ate) was generated; where -Ate
`opened
`and propagated during
`a
`single
`hydraulic
`
`fracture pumping event;
`t/(1+ At/tp), At
`=
`shut-in time
`(days),
`and tp
`
`
`(2) whether proppant would screen out easier
`flowing time, 20 days.
`in a horizontal well;
`
`(3) understanding what determines which natural
`of pressure-squared
`approach
`instead of
`The
`use
`fractures are propagated;
`the
`pseudo pressure for gas
`reservoir analysis. is
`fracture diagnostic
`(4)
`determining the best
`proven
`to
`be valid for
`reservoir pressures
`less
`system to use in a horizontal well;
`than 2000 psia.
`A Flopetrol Johnson/Schlumberger-type
`(5)
`understanding
`how
`to
`curve was
`used for
`infinite acting reservoir with
`
`and the volumes required;
`double
`porosity
`behavior
`(pseudo
`steady
`state
`
`pad
`need or value of
`(6)
`understanding the
`interporosity flow), wellbore
`storage,
`and
`skin.
`
`
`the
`volumes when
`treating multiple
`fractures
`at
`The permeability was calculated from match points
`
`
`same time.
`at
`.492 md and skin factor was calculated at 1.386.
`
`Using
`the Horner
`technique,
`the
`permeability was
`The overall
`technical approach was to:
`.327 md,
`average reservoir pressure was
`177 psia,
`and skin factor was
`-0.881.
`The Rectangular Hyper-
`bolic Method
`(RHM) was
`also utilized to estimate
`the
`various
`reservoir
`properties.
`The
`computed
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`place
`
`proppants
`
`
`
`
`
`
`
`
`
`
`
` (1)
`induce multiple
`hydraulic
`fractures,
`
`
`both controlled and uncontrolled;
`
`
`
`03‘2t"3f 14
`
`
`
`03 of 14
`
`

`
`PRODUCTION AND STIMULATION ANALYSIS OF
`SPE 19090
`MULTIPLE HYDRAULIC FRACTURING OF A 2000-FOOT HORIZONTAL WELL
`
`
`how many
`determine
`(2)
`were induced in the borehole;
`fracture
`(3)
`evaluate
`hydraulic
`a horizontal well
`in shale formation;
`,
`(4)
`establish need or lack of need for proppant
`in low stress ratio (minimum horizontal
`to vertical)
`areas.
`
`design
`
`for
`
`and where
`
`fractures
`
`open
`Initial
`wellbore.
`declined rapidly so that
`baseline rate after 20 days.
`
`80 mcfpd
`of
`flow rate
`the well was making the
`
`also
`stimulation was
`full-scale
`second
`The
`conducted in Zone 1 since it was felt that a better
`comparison of
`fluids would
`be more
`realistic and
`meaningful
`if all
`tests were conducted in the same
`zone.
`The
`second fluid was
`liquid C02, which is
`a cryogenic fluid, pumped at 0°F,
`and at pressures
`about
`200
`psi
`above
`closure
`pressure.
`The
`stimulation was
`conducted
`in
`two
`stages,
`pumped
`at
`two different rates, with considerable difference
`in the results in terms of the number of fractures
`inflated.
`More
`fractures were
`inflated at
`the
`higher injection rates.
`In addition,
`the production
`improvement ratio was higher with C03 when compared
`to nitrogen gas and nitrogen foam as fluids.
`Initial
`production was more than 250 mcfpd, however, after
`more
`than
`50
`days
`of production,
`the
`rate
`had
`declined again to the original
`rate of 2.2 mcfpd.
`One plausible explanation is that without proppant,
`the
`fractures
`opened
`up
`and
`simply
`closed with
`time.
`
`losing production because
`experience of
`This
`of closing fractures led us to conclude that proppant
`was a necessary ingredient in the stimulation design.
`The
`third stimulation was
`a
`small
`volume nitrogen
`foam stimulation pumped
`in
`two
`stages
`(#1
`pad;
`#2 proppant), but at the same rate of 10 bbls/minute.
`Two different
`radioactive
`tracers were
`used
`to
`determine where
`fractures were
`being
`propagated
`along the wellbore.
`Forty—six (46)
`fractures were
`opened and propagated.
`After cleanup,
`the production I
`was sustained due to the use of proppant.
`
`conducted in Zone
`fourth stimulation was
`The
`results of Frac
`4
`combined. After
`the
`and
`2-3
`it was felt
`that we needed to see if a
`large
`#3,
`volume
`fracture
`over
`about
`the
`same
`length of
`wellbore would give
`a proportionate
`increase
`in
`production rate, The large volume fracture consisted
`of 4500 gallons of
`liquid C02 as
`a prepad, 44,000
`gallons of pad,
`and 90,000 gallons of 80-quality
`foam containing 250,000 pounds of sand (2.5 lbs/gal)
`all
`pumped at 50 gallons per minute downhole foam
`rate.
`There were
`some difficult
`sand
`cleanup
`problems
`after
`this
`frac
`job.
`The
`improvement
`ratio of stimulated production to natural production
`was 3.1 to 1.
`Zone
`4 was
`the zone with a high
`natural
`show of 2.16 million scf of gas per day
`and was a major fault and fracture zone.
`A summary
`of
`the
`stimulation treatment
`schedule
`for No.
`4
`is
`shown
`in Table
`3
`and
`the production history
`after stimulation is shown in Figure 3.
`
`a scaled—down
`fracture was
`The fifth and final
`The final
`treatment covered
`version of Frac No. 4.
`almost
`twice as much borehole (930 feet)
`in Zones
`5 and 8 versus 590 feet
`in Zones 2-3 and 4 during
`Frac
`#4,
`but
`pumped
`only
`105,000
`gallons
`of
`85-quality foam and 150,000 pounds of
`sand at
`50
`barrels per minute
`rate.
`Sand cleanout problems
`were
`not
`as
`severe
`this
`time.
`Gas
`production
`improvements ratio for
`the combined zones was 6.1
`to 1, which was
`an
`improvement over Frac
`#4
`in
`Zones 2-3 and 4, but not
`in the same class as Frac
`#3 with its 15.5 to 1
`improvement ratio.
`
`to
`had
`design
`fracture
`hydraulic
`Conceptual
`interaction between the natural
`the strong
`consider
`fracture orientation of N37°E
`and N67°E
`and
`the
`predicted
`induced
`fracture
`trend
`of N52°E.
`In
`addition,
`the consideration of other
`joint
`systems
`having
`nearly
`parallel
`orientations which would
`either
`act
`as
`leakoff
`areas
`or
`actually accept
`fracture fluid under propagating conditions.
`Each
`zone available for stimulation had numerous natural
`fractures which would
`accept
`fracturing
`fluid.
`An open hole type completion technique using external
`casing packers and port collars was used to isolate
`zones with different stimulation potential.
`
`The mechanical
`fracturing fluids,
`handling of
`proppants,
`and
`tracer materials along a
`2000
`foot
`horizontal wellbore offers
`a
`technical
`challenge
`relative
`to developing
`a
`systematic
`approach
`to
`conducting fracturing experiments
`in selected zones
`without causing any permanent damage to the wellbore
`that
`would
`prevent
`execution
`of
`remaining
`stimulations.
`The
`rationale
`used was
`to
`select
`the lowest productive zone(s)
`to conduct experiments
`in and
`subsequently reserve
`the better
`zones
`for
`full-scale stimulation.
`Zones
`6 and 1 were selected
`for
`testing.
`Zone
`6
`had
`very few fractures
`and
`was
`selected for
`the mini
`frac tests, while Zone
`1 had many fractures and was selected for frac fluid
`testing.
`The overall
`stimulation rationale focused
`on the following considerations:
`
`propagate natural
`to
`Primary design was
`(1)
`in orientation
`fractures with a
`slight difference
`from principal stress orientation.
`allows
`(2)
`Injection at
`low rates
`fluid to
`select
`pre-existing
`natural
`fractures
`to
`be
`propa ated.
`(3)
`Injection at
`pressures which will
`the fracture(s) from growing out of zone.
`(4)
`By
`starting off at
`low injection rates
`and not
`exceeding
`200 psi
`above closure pressure
`with
`average
`BHTP,
`natural
`fractures would
`be
`propagated.
`increasing injection rates, additional
`(5)
`By
`fractures would be induced which would likely create
`a
`network
`of
`interconnected
`fractures
`with
`orientations of N37°E, N52°E, and N67°E.
`
`keep
`
`6 using a
`conducted on Zone
`fracs were
`Data
`From this
`computerized‘ data
`acquisition
`system.
`(or
`parting
`series
`of
`tests,
`closure
`pressure
`and
`1050 psi.
`pressure) was determined to be 850
`The
`lower pressure is postulated to be
`the closure
`pressure
`for
`a natural
`fracture,
`and
`the
`higher
`pressure
`for
`an
`induced
`fracture.
`The
`fracture
`gradient was calculated to be 0.25 psi/ft of depth
`for Zone 6.
`The
`ratio of minimum horizontal stress
`to vertical stress was calculated to be 0.22.
`
`on
`five full-scale stimulations
`first of
`The
`the horizontal well was
`conducted on Zone
`1 with
`nitrogen gas
`fluid.
`The gas was
`injected at
`slow
`rates
`to
`inflate
`the
`natural
`fractures
`in
`the
`
`04 olE‘14
`
`04 of 14
`
`

`
`SPE 19090
`
`Albert B. Yost II and William K. Overbey, Jr.
`
`5
`
`A summary of the stimulation treatment schedule
`for No.
`5 is shown in Table 4 and the post-stimulation
`production is shown
`in Figure 4.
`A summary of all
`stimulation treatment
`fluids,
`rates,
`volumes,
`and
`diagnostics is shown in Table 5.
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`Productivity Improvement
`
`in the
`the different frac jobs
`result of
`a
`As
`zones,
`the production was
`enhanced in all
`various
`This
`improvement
`in production is reflected
`zones.
`increase
`in flow rates
`and
`a decrease in
`in
`the
`skin factor values.
`Following stimulation No.
`5,
`frac sand
`and plugs were
`removed
`from the entire
`2000
`foot
`section
`and
`the well was
`placed
`on
`production at
`155 mcfd.
`Both reservoir
`simulation
`and
`average
`current
`day production from 72 wells
`in the field indicate that stimulated vertical wells
`are currently averaging 13 mcfd. Pre-frac stabilized
`flow rate from the horizontal well was
`35 mcfd.
`A
`summary
`of
`individual
`stimulation
`improvement
`ratios
`for
`frac No.
`1
`and 2 went
`to zero beyond
`40 days of flow due to the lack of proppant
`in the
`treatment.
`Overall,
`the productivity improvement
`ratio ranged from -2.9 to 11.8 based on
`40 days of
`production.
`
`in skin value is a qualitative
`improvement
`The
`measurement
`of
`the productivity improvement.
`In
`addition,
`this
`improvement
`is
`indicative
`of
`the
`conditions
`around the wellbore which is translated
`into an
`increase in the surface area contributing
`to production due
`to the
`stimulation process.
`A
`negative skin indicates a stimulated wellbore; hence,
`a successful stimulation.
`
`
`
`
`
`
`
`
`
`
`
`
`a permeability value of
`is believed that
`It
`is
`representative
`of
`the
`formation's
`md
`0.2
`permeability.
`when
`permeability
`anisotropy
`(R)
`equals
`1:1,
`the
`first year's
`average
`production
`rate was projected at 83 mcfd, when R = 1.2 (Kx:Ky),
`the first year's average production rate is projected
`at
`97 mcfd.
`Plots of cumulative production versus
`time
`for different
`anisotropy
`ratios
`are
`shown
`in Figure 6.
`In addition,
`a plot of
`the 20-year
`projected
`production
`rate
`versus
`time
`is
`shown
`in Figure 7.
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`the
`evaluate
`to
`used
`GBDFR model was
`The
`to
`location prior
`production
`from the
`potential
`drilling the Recovery Efficiency Test No.
`1 well
`and was
`also used
`to predict production of
`the
`well after‘ drilling and stimulation was completed.
`Figure
`8 projects
`20 year
`cumulative
`production
`for the RET #1 well utilizing developed parameters
`from well
`testing of
`180 psia pressure.
`Using
`the
`full
`reservoir
`thickness
`of
`247
`feet
`as
`productive reservoir, we found that we had to reduce
`the permeability to an average of 0.09 md
`to match
`the
`current
`rate of production.
`This
`indicates
`that
`there are most
`likely heterogeneities in the
`fracture
`system and
`that
`the
`flow path to the
`wellbore
`is not consistent.
`It
`is
`likely that
`the
`fracture
`permeability changes with
`time
`as
`fractures
`slowly close as pressure declines with
`production.
`This would
`seem to be
`one
`argument
`in favor of holding a back pressure on the formation
`during production.
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`
`Figure 9 compares the final projected production
`and decline curve with the pre—drilling estimate.
`The difference
`in
`the projections was
`primarily
`the difference in pressures used.
`The pre—drilling
`pre-stimulation
`the
`horizontal well,
`the
`In
`skin value was estimated at -2.87 due to the geometry
`model
`used 350 psi
`reservoir pressure, while the
`of
`the wellbore (horizontal well),
`since horizontal
`post—drilling projection used 180 psia. Pre-drilling
`model studies also projected a vertical well, drilled
`wellbores
`are equivalent
`to stimulated reservoirs.
`at
`the site where the horizontal well was drilled.
`The
`skin values
`showed
`an
`improvement
`for Zones
`1, 2-3, and 4, whereas a decrease in skin from -2.87
`would produce 80 mmcf
`in 20 years.
`This comparison
`to -0.881 was detected in Zones
`5 and 8. This could
`indicates
`the horizontal well
`should produce 7.8
`times more
`gas
`than a vertical well drilled at
`be
`due
`to presence of
`sand
`in
`the wellbore or
`
`
`
`
`the same location.
`formation damage as a result of the frac job.
`
` An additional method of analyzing stimulation
`CONCLUSIONS
`
`effectiveness
`is
`the
`examination
`of permeability
`improvements.
`Table 7 provided data on the post—frac
`1.
`This
`2000
`foot horizontal well
`in fractured
`
`permeability compared to the pre-frac permeability.
`Devonian
`shale
`has
`successfully demonstrated
`
`Improvements
`ranged from 1.79 to 4.4 with an average
`numerous
`folds of
`increase
`in production as
`ratio of 3.2.
`
`
`compared to vertical wells in a pressuredepleted
`
`producing field.
`
`
`The production decline curve for the horizontal
`is
`shown
`in Figure
`5.
`The
`stabilized flow
`well
`rate was
`95 mcfd representing a 2.7 fold increase
`as
`a result of hydraulic fracturing.
`The horizontal
`well
`is currently producing 7
`times more
`than a
`
`
`vertical well
`based on
`simulation and the 72-well
`
`average flow rate for the field.
`
`2.
`
`3.
`
`
`
`
`
`
`
`
`
`
`
`to predict/projec
`used
`GSDFR model was
`The
`a 20-year history of production based on estimated
`values of
`reservoir pressure,
`formation thickness,
`
`
`horizontal drilling and multiple
`long
`Both
`and
`average
`permeability.
`The
`average
`reservoi
`are
`required
`to
`achieve
`high
`stimulations
`pressure and formation thickness were kept
`constan
`folds of increase in production.
`at 182 psia and 247 feet,
`respectively, due to th
`
`fact
`that
`geologic
`and
`engineering
`data wer-
`sufficient
`to
`accurately
`estimate
`these
`values.
`
`Post-stimulation
`permeability
`was
`calculated
`to
`
`be 0.200 md.
`
`
`0525)f 14
`
`4.
`
`
`
`
`
`
`
`
`
`
`successfully
`were
`improvements
`Productivity
`actual
`flow rates,
`build—up
`evaluated
`by
`analysis, and skin factor calculations.
`
`the most extensively
`represents
`This project
`documented
`zone-to—zone production and stimu-
`lation testing of
`a
`long horizontal well
`in
`a naturally-fractured gas reservoir.
`
`05 of 14
`
`

`
`6
`
`REFERENCES
`
`PRODUCTION AND STIMULATION ANALYSIS OF
`MULTIPLE HYDRAULIC FRACTURING OF A 2000-FOOT HORIZONTAL HELL
`
`SPE 19090
`
`1.
`
`"Natural
`Pasini, J. III, and W.K. Overbey, Jr.
`Their
`and
`Induced
`Fracture
`Systems
`and
`Application to Petroleum Production." SPE Paper
`2565
`presented
`at
`SPE Meeting
`in Denver,
`Colorado,
`(May, 1969).
`
`and Glenn, E.E.,
`Strubhar, M.K., Fitch, J.L.,
`Jr.
`"Multiple, Vertical
`Fractures
`from an
`Inclined Wellbore -- a Field Experiment," Paper
`SPE
`5115
`presented
`at
`SPE-AIME
`49th Annual
`Fall Meeting, Houston,
`Texas, October
`6-9,
`1974.
`
`“Drilling
`and w.M.~ Ryan.
`Jr.
`Overbey, M.K.,
`Stimulate
`a Directionally Deviated well
`to
`Gas Production
`from a Marginal Reservoir
`in
`Southern Nest_Virginia,” MERC/TPR-76/3 (1976).
`
`"Drilling
`R.N. Metzler.
`and
`G.R.
`McManus,
`Stimulate
`-a Directionally Deviated well
`to
`Gas Production from a Marginal Reservoir Near
`Cottageville, West Virginia,"
`Final
`Report
`Under ERDA Contract E(461)-8047 with Consolidated
`Gas Supply Corporation (1979).
`
`.
`
`.
`
`Yost, A.B. II, w.K. Overbey, Jr., D.A. Wilkins,
`and C.D.
`Locke.
`"Hydraulic Fracturing of
`a
`Horizontal
`Well
`in
`a
`Naturally-Fractured
`Reservoir:
`Case Study
`for Multiple Fracture
`Design".
`SPE Paper
`17759,
`presented at Gas
`Tehcnology Symposium, June, 1988.
`.
`'
`and D.A.
`II,
`Overbey, w.K., Jr., A.B. Yost
`Wilkins.
`"Inducing Multiple Hydraulic Fractures
`from a Horizontal Nellbore“,
`SPE Paper 18249,
`presented at 63rd Annual Technical Conference,
`Houston, Texas, October 2-5, 1988.
`
`"Pressure Build-
`and Kabir, C.S.
`.- Hasan, A.R.
`A- Simplified Approach",
`JPT,
`up Analysis:
`January 1983, 178-188.
`
`Salamy, S.P., C.D. Locke, w.K. Overbey, Jr.,
`A.B. Yost II.
`"Four Pressure Build-up Analysis
`Techniques Applied to Horizontal
`and Vertical
`Wells with Field Examples,"
`SPE
`#19101, pre-
`sented at
`the Gas Technology Symposium, Dallas,
`Texas, June 7-9, 1989.
`
`Table 1
`
`I
`
`
`
`Pre—Stimulation Pressure Build—Up and Drawdown Test Results
`Flet N0. 1 — Wayne County, West Virginia
`
`Length
`__C_)_fi-
`
`
`
`24-Hour
`Build—Up
`3&1
`
`Permeabi|ity*
`_i_n_id)_
`
`Flow Rate”
`_imm)_
`
`404
`
`417
`
`182
`
`640
`
`135
`
`90
`
`292
`
`54
`
`75
`
`68
`
`73
`
`74
`
`74
`
`83
`
`A
`
`0.031
`
`0.078
`
`0.098
`
`0.073
`
`0.078
`
`0.037
`
`0.068
`
`2.2
`
`4.4
`
`16.7
`
`4.4
`
`2.2
`
`0
`
`5.2
`
`TOTAL:
`
`35.1 mcfd
`
`* Predicted by reservoir simulation model GSDFR
`** 24-hour flow rate test after pressure build-up test
`
`06 0312514
`
`06 of 14
`
`

`
`35 19090
`
`Comparison of Pre— and Post—Frac: Testing Results
`
`
`Table 2
`
`Pre-Frac
`Pressure)
`(24 hr)
`Eulld-Up
`(psla)
`
`Pre-Frac
`Permeablllty
`K (md)
`
`Post-Frac
`Reservolr
`Pressure
`(P518)
`
`Zone{s)
`
`Posl-Frac
`Permeability
`K (md)
`
`P091-Frac
`Skin
`Value
`
`Pre-Frat:
`Flow Rate
`(mnlpd)
`
`Post-Frac
`Flow Rate
`(mdrpd)
`
`0.20""
`0.1835
`0.0477
`0.0480
`0.0900
`
`-----
`
`-3 .21 2
`
`0.1505
`
`-4.220
`
`34.0
`2 .2
`2.2
`2.2
`2.2
`
`21 .1
`
`0.3270
`
`-0.831
`
`9.6
`
`155.0
`009.0
`011.0
`055.0
`034.0
`
`062.0
`
`050.0
`
`1 1 9‘
`74
`54
`54
`54
`
`75
`68
`
`73
`83
`
`0.082***
`0.0792
`0.0306
`0.0306
`0.0306
`
`it
`
`0.084
`
`o.o71**
`
`NA
`NA
`NA
`182
`184
`
`182
`
`178
`
`All
`
`6 1 1 1 2
`
`-3
`
`45 8
`
`Frac
`Number
`
`0
`
`1 .
`2 (N2)
`3 (C02)
`4 (N2 Foam)
`
`5
`
`' Dela from 28-day hulld-up (169 psla boltomhala rassure
`recordad: 192 psla pr
`ujacled as absolute reserv Ir pressure)
`" Weighted average at Individual iesls
`"' Homer plot calculallon
`/
`
`
`TABLE 3. Treatment Schedule for Stimulation No. 4
`
`
`Cumulative
`Sand
`Volume
`Volume _
`allons
`lbs
`
`Sta e
`
`Rate
`b m
`
`Volume
`bbl
`
`Pressure
`:5.
`
`Pump Time
`minutes
`
`a
`22
`
`1‘
`2
`
`3 .
`
`4
`
`5
`
`6
`
`7
`
`8
`
`.
`
`15
`50
`
`40
`
`40
`
`40
`
`40
`
`30
`
`30
`
`119_ (co,)
`1, 140
`
`119
`
`119

This document is available on Docket Alarm but you must sign up to view it.


Or .

Accessing this document will incur an additional charge of $.

After purchase, you can access this document again without charge.

Accept $ Charge
throbber

Still Working On It

This document is taking longer than usual to download. This can happen if we need to contact the court directly to obtain the document and their servers are running slowly.

Give it another minute or two to complete, and then try the refresh button.

throbber

A few More Minutes ... Still Working

It can take up to 5 minutes for us to download a document if the court servers are running slowly.

Thank you for your continued patience.

This document could not be displayed.

We could not find this document within its docket. Please go back to the docket page and check the link. If that does not work, go back to the docket and refresh it to pull the newest information.

Your account does not support viewing this document.

You need a Paid Account to view this document. Click here to change your account type.

Your account does not support viewing this document.

Set your membership status to view this document.

With a Docket Alarm membership, you'll get a whole lot more, including:

  • Up-to-date information for this case.
  • Email alerts whenever there is an update.
  • Full text search for other cases.
  • Get email alerts whenever a new case matches your search.

Become a Member

One Moment Please

The filing “” is large (MB) and is being downloaded.

Please refresh this page in a few minutes to see if the filing has been downloaded. The filing will also be emailed to you when the download completes.

Your document is on its way!

If you do not receive the document in five minutes, contact support at support@docketalarm.com.

Sealed Document

We are unable to display this document, it may be under a court ordered seal.

If you have proper credentials to access the file, you may proceed directly to the court's system using your government issued username and password.


Access Government Site

We are redirecting you
to a mobile optimized page.





Document Unreadable or Corrupt

Refresh this Document
Go to the Docket

We are unable to display this document.

Refresh this Document
Go to the Docket