throbber
A Unique Method for
`Perforating, Fracturing, and
`Completing Horizontal Wells
`
`A.P. Damgaard, SPE, Maersk Energy Inc., and D.S. Bangort, SPE, D.J. Murray, R.P. Rubbo,
`SPE, and O.W. Stout,* SPE, Baker Oil Tools
`SPE 19282
`Summary. This paper describes the evolution, laboratory testing, and field installation of a completion system developed to per-
`forate, fracture stimulate, and isolate multiple zones in North Sea horizontal wells. This system is designed to reduce overall completion
`time and well control problems significantly and to allow selective zone control in production and restimulation phases. The field per-
`formance of this system is compared with that of previously used methods.
`
`Background
`Maersk Oil & Gas A/S began drilling horizontal wells in the Dan
`field in 1987 with the primary goal of improving productivity in
`the low-permeability chalk. A feasibility study concluded that a
`matrix-acidized horizontal well would yield a productivity equal
`to or slightly better than that of a successfully propped, hydrauli-
`cally fractured conventional well, albeit at a higher cost.1 There-
`fore, to make horizontal wells economically attractive, fracture
`stimulating multiple zones in the drainhole section would be nec-
`essary. Before the use of this new technique, three Dan field horizon-
`tal wells—Wells MFB-14, MFB-15, and MFB-13—were completed
`with multiple fracture stimulation treatments. Production experi-
`ence from these three horizontal wells confirmed that production
`increases by a factor of three to four over that of a conventional
`well. Thus, the decision was made that further field development
`would be based mainly on multiple fractured stimulated horizontal
`wells.
`
`Completion Experience With Existing Horizontal Wells. Suc-
`cessful liner installation and cementation is considered a prerequi-
`site to ensure adequate zonal isolation for multiple fracture
`treatments in horizontal wells. The radius of curvature for both the
`short- and medium-radius methods (33 to 50 ft and 300 ft, respec-
`tively) would make successful liner cementation difficult. For this
`reason, the long-radius directional drilling method was considered
`to be the most attractive option.
`Although the first horizontal well (Well MFB-14) was equipped
`with a 51/-in. liner across the reservoir, 7-in. liners have been in-
`stalled in subsequent wells to allow more flexibility in the selec-
`tion of perforating and stimulation tools.
`Because an initial concern was that the annular area between the
`7-in. liner and the 81/2-in.-diameter hole would be insufficient for
`a good cementation job, 63/4-in. liners were considered as an op-
`tion. A Cement Evaluation Toolsm , Variable Density Log sm , and
`gamma ray and casing-collar locator logs run in all Dan field
`horizontal wells indicated that zonal isolation had been achieved
`with the 7-in. liners that had been well centralized and rotated dur-
`ing cementation. This was confirmed during execution of fractur-
`ing jobs where no communication between individual fractures was
`observed.
`
`Previous Perforating/Sdmulating Techniques. The following ab-
`breviated history of completion systems used in previous Dan
`horizontal wells corroborates the need for an improved comple-
`tion system for multiple stimulated horizontal wells.
`Well MFB-14 was perforated and stimulated with the following
`procedure (see Fig. 1).
`1. The zone was perforated and stimulated with a conventional
`drillstem test string.
`2. After the well was killed with brine and losses were cured with
`lost-circulation materials, a bridge plug was set above the zone.
`•Now at The Western Co.
`CoPYtIght 1902 Society of Petroleum Engineers
`
`SPE Production Engineering, February 1992
`
`3. The next zone was perforated, stimulated, and tested.
`4. After the well was killed, the bridge plug was milled and
`pushed to bottom, and a new bridge plug was installed above the
`latest set of perforations, after which a new zone could be perfo-
`rated and stimulated.
`This procedure required three trips to stimulate one zone. This,
`together with problems with curing losses and gains experienced
`when the bridge plugs were milled and pushed to bottom, resulted
`in an excessive total stimulation time.
`To reduce time during the perforating and stimulating operations,
`a straddle packer assembly (Fig. 2) was used successfully on the
`second horizontal well, Well MFB-15. This well was stimulated
`with acid without proppant. To maintain well control during trip-
`ping, it was necessary to flow each zone after the stimulation be-
`cause of the 300- to 400-psi supercharging from the stimulation
`fluids.
`A new packer assembly was designed for stimulation of Well
`MFB-13. The objective of the new design was to enable isolation
`of the fractured zone immediately after stimulation to prevent the
`gain/loss situation experienced in Well MFB-15. This would be
`achieved by placing the retrievable bridge plug above the last treated
`interval while picking up a new tubing-conveyed perforating (TCP)
`assembly. Fig. 3 shows this tool string. Two different bridge plugs,
`one inflatable and the other mechanical, were used, with some oper-
`ational problems.
`
`Dovolopmont of Method
`Cost and Performance Objectives. Drilling and completion of
`Welts MFB-14, MFB-15, and MFB-13 were finalized in mid-1988.
`An operations review showed that the scope for significantly im-
`proving drilling time was limited, but there was a potential for sig-
`nificantly reducing completion time and associated costs. Therefore,
`the decision was made to design completion tools/techniques for
`horizontal wells with the following objectives: (1) to reduce stimu-
`lation and completion time for both acid fracturing and propped
`hydraulic fracturing; (2) to reduce or eliminate losses of expensive
`completion fluids and thereby improve well control during com-
`pletion operations; (3) to allow selective restimulation of the in-
`dividual zones without a drilling rig or workover hoist; and (4) to
`permit isolation of or to shut off zones producing excessive amounts
`of gas.
`
`Completion System Development. With a thorough understand-
`ing of the desired completion system characteristics, the designers
`conceived numerous alternatives, ranging from modifications of ex-
`isting techniques to novel methods that would require extensive de-
`velopment. Four of the most viable alternatives were developed
`to a degree sufficient to project the performances and characteris-
`tics of the systems. For each concept, a proposed completion pro-
`gram was generated that described each required operational step
`in sequential order. A performance matrix comparing the relative
`merits and disadvantages of each system was also produced. Fi-
`nally, an economic analysis covering total projected costs for each
`
`1 of 9
`
`61
`
`Ex. 2079
`IPR2016-01496
`
`

`

`O
`
`BRIDGE PLUG,
`MILLED AND
`PUSHED TO
`BOTTOM
`
`WORKING
`STRING
`
`PERFORATED
`JOINT
`
`
`
`1,
`RODUCT1ON
`LINER
`
`AAA
`
`TCP
`N
`
`A
`
`N
`
`\--- SAND FILLED
`FRACTURES
`
`50x SW
`
`PLANNED PERFORATING
`INTERVAL
`
`PACK ER
`
`BRIDGE
`
`Fig. 1—Stimulation with millable bridge plugs.
`
`\\\\9 ii/r cam
`
`TOP CHALK
`
`WORKING
`
`STRADDLE
`PACKER
`
`PRODUCTION
`LINER
`
`AAA
`
`50% SW
`
`PLANNED PERFORATING
`INTERVAL
`
`CIRCULATION
`VALVE
`
`TCP
`GUN
`
`FRACTURES
`
`A
`sun-
`
`L CM
`MATERIAL
`PLUG
`
`Fig. 2—Stimulation with straddle packer.
`
`option was conducted. This analysis included, but was not limited
`to, hardware procurement, expense of performing each operation,
`and potential cost of fluid losses. The analysis indicated that the
`option selected addressed each performance objective, offered to-
`tal cost advantages, and was based on proven technology. The op-
`tion selected was the perforate, stimulate, and isolate (PSI) system.
`
`PSI System Description
`The completion system selected for development was designed to
`permit each interval to be perforated, stimulated, and isolated in
`a single workstring trip. This system consists of three basic assem-
`blies: a permanent sump packer with bull-plugged bottom (Fg. 4),
`a downhole assembly for isolating each interval after treating and
`permitting selective production or stimulation (Mg. 5), and a serv-
`ice assembly for perforating and stimulation operations (Fig. 6).
`The downhole and service assemblies are made up with the 214 -
`in. concentric workstring and TCP gun assembly installed concen-
`trically inside the downhole assembly (see Fig. 7). These two com-
`ponents are run into the well simultaneously. Following perforation
`and stimulation operations, the downhole assembly is positioned
`and set in a manner to isolate the perforations; then the service as-
`sembly is retrieved from the wellbore.
`After all zones are isolated and the production tubing string is
`installed, a coiled-tubing-conveyed manipulation tool string is run
`in to open the sliding sleeves. The tool string can be run at any
`time in the future to close off any zone or to reopen a zone that
`was previously closed. The tool string includes a:backflow valve,
`an emergency release device, and a washing device to dean out
`the sliding sleeves before they are moved.
`
`62
`
`Downhole Assembly. The downhole assembly consists of three
`main parts (see Fig. 5). The first is a locator seal assembly used
`to provide pressure integrity between the sump packer and the down-
`hole assembly. The second component is a sliding sleeve used to
`provide selective production control. The third is a hydraulically
`set, retrievable isolation packer.
`A 41/4-in.-OD, 12.6-lbf/ft L-80 tubing with premium threads is
`made up between the seal assembly and the sliding sleeve. This
`section typically is 20 to 80 ft long.
`The sliding sleeve, which is run in the closed position, contains
`a sleeve valve that can be opened by shifting upward and closed
`by shifting downward with a coiled-tubing-conveyed manipulation
`tool string.
`An additional length of 41/4-in.-0D, 12.6 lbf/ft L-80 tubing with
`premium threads is made up between the sliding sleeve and the iso-
`lation packer. The length of this section is governed by interval
`spacing, but it typically ranges from 200 to 400 ft.
`The last component in the downhole assembly is a hydraulically
`set, retrievable isolation packer. This packer contains a sealbore
`that will accept seal assemblies. The isolation packer's setting piston
`is hydraulically balanced to prevent presetting. It cannot be set un-
`til the locator seal assembly has been stabbed into the sump packer.
`
`Service Assembly. The service assembly contains five main com-
`ponents (Fig. 6). The lowermost consists of 20-ft-long, 31/4- or 3 %-
`in.-OD TCP guns and firing head. The firing head is actuated by
`hydraulic pressure. After actuating, there is a time delay before
`detonation to permit underbalanced perforating if desired.
`The second component is a mechanism that automatically retracts
`the TCP guns and firing head to a position inside the downhole
`
`SPE Production Engineering, February 1992
`
`2 of 9
`
`Ex. 2079
`IPR2016-01496
`
`

`

`\\\\9 5/B" CASING
`
`WORKING
`STRING
`
`PERFORATED
`JOINT
`
`TOP CHALK
`
`SOC
`
`PRODUCTION
`LINER
`a a
`
`TCP
`GUN k OVERSHOT
`
`FRACTURES
`
`50s SW
`
`PLANNED PERFORATING
`INTERVAL
`
`PACKER
`
`RETRIEVABLE
`
`BRIDGE
`PL
`UG
`
`Fig. 3—Stimulation with retrievable bridge plugs.
`
`CASINO
`T" O.D.
`
`Fig. 4—Setting sump packer.
`
`assembly after perforating. The TCP guns are retracted to allow
`full circulation and thus to avoid sticking problems should a prema-
`ture screenout occur during fracturing.
`The third component is a circulation device that allows fluid to
`flow from the workstring ID through the annular space around the
`perforating guns and into the lower casing annulus.
`A length of 236-in.-OD concentric workstring is used to separate
`the lower three service assembly components from the upper com-
`ponents. This workstring is also used to space the TCP guns, fir-
`ing head, and gun retractor so that the TCP guns are positioned
`below the seal assembly after the downhple and service assemblies
`are connected.
`The fourth component in the service assembly is the disconnect
`sub. It is used to make a pressure-tight, rotationally locked, me-
`chanical connection between the service assembly and the down-
`hole assembly. The upper end of the 2% -in. tubing is suspended
`from the disconnect sub. The two assemblies are disconnected with
`30,000 lbm tension.
`The fifth component is a mechanically operated stimulation packer
`whose design is based on standard compression-set squeeze tools.
`The conventional rotational control system used during setting and
`releasing operations was replaced by an automatic J-slot control
`system, which is operated with 21/2 ft of reciprocation. This pack-
`er is run immediately above the disconnect sub and is attached direct-
`ly to the workstring.
`
`Operational Procedures. The basic operational procedures used
`with this completion system are as follows.
`1. Run the bull-plugged sump packer on drffi- pipe and set it
`hydraulically at a point below the bottom interval (see Fig. 4). Pull
`the drillpipe and setting tool.
`2. Make up the downhole assembly and temporarily suspend it
`from the rotary table.
`
`SPE Production Engineering, February 1992
`
`TUBING
`
`LOCATOR
`SEAL MISSIZI
`
`pnatrixiornt norm Kroabr
`Fig. 5—Downhole assembly.
`
`3. With a gravel-pack screen-handling table (false rotary table),
`run the lower portion of the service assembly through the down-
`hole assembly ID. Run the service assembly until the disconnect
`sub can be made up into the top of the downhole assembly's isola-
`tion packer. The TCP guns will be spaced below the locator seal
`assembly at this time.
`4. Run the combined assemblies to perforating depth (see Fig.
`7) and set the stimulation packer by picking up 2 1/2 ft at the packer
`and then slacking off 10,000 lbm.
`5. Pressure the workstring to actuate the TCP guns. Guns will
`automatically retract after firing (see Fig. 8).
`6. Stimulate according to the program (Fig. 9).
`7. Pick up and release the stimulation packer. Establish reverse
`circulation and slack off to remove any proppant remaining inside
`the casing (Fig,. 10).
`8. Stab the seal assembly into the sump packer and pressure the
`workstring to 6,000 psi to set the isolation packer (see Fig. 11).
`9. Bleed the pressureand pick up the workstring 30,030 lbm over
`string weight to disconnect the service assembly from the down-
`hole assembly (Fig. 12). Retrieve the service assembly.
`
`3 of 9
`
`63
`
`Ex. 2079
`IPR2016-01496
`
`

`

`CIRCULATION
`OEM
`
`CrOrTnameL
`r
`
`SERVICE MCMINN
`DISCONNECT
`
`col-1 Luton
`lop
`RETRACTOR
`(=NM ecemon)
`Fig. 8—Service assembly.
`
`WORK SUNG
`
`Fig. 7—Running In hole.
`
`GU
`IWCTED)
`OKT
`
`SUN
`
`(RI OCTINKITRCASMON)
`
`Fig. 8—Perforated.
`
`Fig. 9—Stimulating.
`
`10. Repeat Steps 2 through 9 until all intervals have been perfo-
`rated, stimulated, and isolated by stacking the required number of
`downhole assemblies on top of one another.
`11. Make up and run production tubing and completion equip-
`ment as required. Land the production-tubing seal assembly in the
`sealbore of the uppermost isolation packer.
`12. Run and land the tubing banger. Make up the wellhead.
`Sliding-Sleeve Manipulation. The sliding sleeves are shifted open
`to commingle the stimulated zones with a shifting tool carried on
`coiled tubing. Before the sliding sleeves are shifted, a separate
`coiled-tubing run is made to wash out any debris that may have
`accumulated in the sliding-sleeve profiles during completion.
`1. Wash run. Run in the hole, maintaining circulation until just
`above the first sliding sleeve. Increase the pump rate to about 1
`bbl/min and continue down to bottom. Then pull out, continuing
`to wash until out of the horizontal section.
`
`2. Opening the sliding sleeves. Run down the vertical section of
`the well, maintaining sufficient pressure to allow circulation. Be-
`fore the horizontal section is reached, increase the pump rate to
`about 1 bbl/min and continue down to total depth (TD). Pull up
`to the first sliding sleeve until the shifting tool engages; then con-
`tinue pulling to open the sleeve. After a few seconds, the weight
`indicator will slowly drop off, indicating that the sliding sleeve is
`opening. Repeat this procedure at each sliding sleeve until all slid-
`ing sleeves are open.
`
`Summary of Component and System Tests. It is standard prac-
`tice to test new equipment thoroughly before introduction in the
`field. The first problem encountered during test preparation of the
`PSI system was that all the test facilities were designed for vertical
`completions. Simulation of horizontal well conditions required the
`fabrication of a 7-in.-casing horizontal test fixture with adequate
`
`64
`
`4 of 9
`
`Ex. 2079
`SPE Production Engineering, February 1992
`IPR2016-01496
`
`

`

`NETINEWALE
`SE
`PACXERRIMEET)
`
`Fig. 10—Reversing.
`
`NETINEMVILE
`PACISMCCEUNSET)
`
`NETRIENPOLE
`COMPLETION
`tAgcER
`
`Fig. 11—Setting completion packer. .
`
`Fig. 12—Isolated with workstring removed.
`
`space around it for running tools in and out of the fixture. This
`particular fixture did not include a curved section to simulate a build
`angle because this completion was to have a maximum build of only
`6°/100 ft. The 7-in. test fixture was about 120 ft long. A hydraulic
`manipulator was made up to one end of the casing, with a test cap
`at the opposite end. The hydraulic manipulator was a long-stroke
`hydraulically actuated piston to provide back-and-forth motion of
`the components in the PSI system. The test cap and hydraulic
`manipulator allowed application of annulus or tubing pressure to
`simulate downhole conditions. The hydraulic manipulator also al-
`lowed simulation of the application of set-down weight or pickup
`tension from the rig floor.
`Component Tests.
`1. The service packer was set and released in the horizontal po-
`sition. An 8,000-psi pressure test at ambient temperature and 220°F
`was performed.
`2. The isolation packer was set, pressure tested to 7,500 psi at
`ambient temperature and 220°F, and retrieved.
`3. Swab-off tests to determine circulation limits were performed
`on both packers.
`4. The automatic gun retractor was actuated with 5,000-psi nitro-
`gen as the driving medium.
`Complete PSI System Tests With the Horizontal Test Fixture.
`1. Set bull-plugged sump packer on a hydraulic setting tool.
`2. Made up the entire assembly for one zone (see Fig. 7) with
`only one joint of 41/2-in. tubing.
`3. Set the service packer.
`4. Pressure tested to 5,000 psi from above.
`5; Simulated gun detonation and actuated gun retractor.
`6. Simulated screenout conditions against the service packer by
`pressuring tubing to 7,500 psi.
`
`SPE Production Engineering, February 1992
`
`7. Released service packer.
`8. Stroked hydraulic actuator in to land locator seal assembly in
`sump packer, which was set in the bottom of the test fixture.
`9. Pressure tested the upper annulus to 2,000 psi to verify seal
`integrity.
`10. Set the isolation packer.
`11. Pressure tested the isolation packer to 7,500 psi both above
`and below.
`12. Pulled disconnect sub from the isolation packer and removed
`the service assembly.
`13. Shifted the sliding sleeve open and then closed it.
`14. Released the isolation packer with the retrieving tool and
`pulled the isolation string from the fixture.
`As a result of these tests, the equipment was deemed ready for
`field runs in nonpropped stimulation applications.
`A sand-slurry fracture test of the equipment was also conducted
`to evaluate the suitability of the equipment in situations where prop-
`pant might be required. Tools were assembled and installed in the
`7-in.-casing horizontal test fixture. The slurry was circulated through
`the tools until a total of about 600,000 lbm of sand was pumped
`at a rate of 30 bbl/min through the test fixture. Fresh water was
`then circulated through the fixture to remove most of the sand. The
`equipment assembly was then pulled from the 7-in. casing. Exami-
`nation of the tools indicated that turbulence caused erosion around
`the holes and joints over which the slurry had passed.
`It was concluded that some special attention must be given to these
`areas before this system could be used to conduct sand fracturing
`operations in one trip per zone. Sand fracturing operations currently
`must be performed with the PSI system by perforating in one trip
`and running the service (less TCP assembly and gun retractor) and
`downhole assemblies in a second trip on drillpipe.
`
`5 of 9
`
`Ex. 2079
`IPR2016-01496
`
`

`

`TUBING HANGER
`
`LOCATOR TUBING SEAL
`ASSEMBLY (TYP.)
`
`ISOLATION PACKER (TYP.)
`
`SLIDING SLEEVE (TYP.)
`ZONE 8
`
`O
`
`0
`
`ZONE 7
`
`O
`
`0
`
`ZONES
`
`O
`
`0
`
`ZONES
`
`SIDE POCKET MANDREL
`
`O
`
`0
`
`ZONE 4
`
`EXPANSION JOINT
`
`RETRIEVABLE SEAL
`BORE PACKER
`
`LINER HANGER
`
`O
`
`0
`
`ZONE 3
`
`ZONE 2
`
`ZONE I
`
`SUMP PACKER
`BULL PLUG
`
`Fig. 13—Horizontal-wall completion.
`
`Application Summary
`Installation Review. All completion equipment was function test-
`ed, made up in 30- to 40-ft-long subassemblies with tubing pup joints
`in each end for easy handling, and subsequently pressure tested to
`the required pressure. After the logs for Well MFA-13 were evalu-
`ated, plans were made to complete the well with eight zones, all
`to be acid fractured. Actual completion operations began by run-
`ning of the sump packer.
`The first makeup of the PSI system was time-consuming, requiring
`about 8.5 hours. Two initial attempts to run the PSI system on the
`nonrotational service packers were not successful because the as-
`sembly would not enter the top of the 7-in. liner from the 9%-in.
`casing. After the liner top was dressed, a different service packer
`was chosen and the procedure described below was followed.
`1. Run the PSI system in the hole on 31/2- and 5-in. drillpipe to
`perforating depth and set the service packer.
`2. Rig up the fracturing tree and lines.
`3. Test the string against the ball valve.
`4. Cycle the ball valve to the circulation position and displace
`the string to filtered seawater.
`
`5. Cycle the ball to test position and pressure up to activate the
`TCP guns.
`6. Rig up the fracturing lines and stimulate the zone.
`7. Cycle the ball valve to the circulation position and reverse out
`seawater (displacement fluid).
`8. Rig down the fracturing tree. Rig up the drillpipe/circulating
`head and pressure test to 6,000 psi.
`9. Unset the service packer and engage seals into the previous
`isolation packer.
`10. Set the isolation packer by applying 6,000-psi surface
`pressure.
`11. Release the service packer from the downbole assembly and
`pull out of the hole.
`The installation of the first five zones was fairly uneventful ex-
`cept for a minor failure of the service packer and the ball valve.
`On the basis of increasing experience, the time between fracturing
`was continuously reduced and actual waiting time on the stimula-
`tion vessel resulted from haitor trips for chemical reloadings.
`A leak was observed during installation of the isolation packer
`for isolation of Zone 6. A pressure test of the =ulna indicated
`
`66
`
`6 of 9
`
`Ex. 2079
`SPE Production Engineering, February 1992
`IPR2016-01496
`
`

`

`I l I
`LEGEND
`TYPE 1- Tripping 'Time
`TYPE 2- Stimulating Tins
`
`TYPE S- Failure Time
`
`TYPE 4- WaitingTim•
`'
`
`TYPE 6- Other Tine
`
`TYPE 6- Find Completion Mom .
`TYPE 7- CoMd Tubing Time
`
`.
`.
`
`-
`
`-
`
`Time (Hours)
`I WU :
`
`900 : c'' \
`800 :
`\
`700:
`600 .
`
`!,1
`4
`,
`-
`500 :
`:4 '
`II
`400:
`
`i '
`'NI
`300 :
`N
`:
`200:
`• .
`'4
`:
`
`1 00 . :
` r
`V
`/0
`N
`442 N
`Si
`e.
`t4
`N
`%,_ 0 0
`laPICL
`• WITTim4L
`TY E 1 TYPE 2 TYPE 5 TYPE 4 TYPE 1 TYPE 6 TYPE 7
`P
`O.
`E
`922
`upsaj.zeisse
`
`,
`
`N
`
`273
`
`57
`
`0
`
`94
`
`311
`
`92
`
`0
`
`4
`
`MFB-13, 7-Zonse
`
`ng
`
`130
`
`111FA-13,11-Zonee
`
`egg
`
`17
`
`40
`
`43
`
`160
`
`121
`
`0
`
`23
`
`206
`
`50
`
`20
`
`61
`
`0
`se
`
`Fig. 14A—Completion-time comparison chart.
`
`>
`
`
`
`• MFB-15
`
`• MFB-13
`
`MFA-13
`
`0
`
`4
`
`6
`
`8
`
`10
`
`12
`
`14
`
`Brine Loss (BBLs x 1000)
`
`Fig. 1413—Fluid loss.
`
`frill packer integrity, indicating that the leak point was somewhere
`in the 41/2-in. isolation string, most likely in the seal assembly or
`the sliding sleeve.
`After the service assembly was released and retrieved, an un-
`successful attempt to release the isolation packer was made with
`the dedicating retrieving tool.
`During these operations, significant losses occurred and further
`attempts to retrieve the isolation assembly from Zone 6 were abort-
`ed. To cure the losses and allow perforation and stimulation of the
`two remaining zones, a short assembly consisting of an isolation
`packer, tubing, and a nipple profile with a blanking plug was in-
`stalled on top of the isolation assembly.
`Perforation and stimulation of the two zones were also fairly un-
`eventful except for one failure of the service packer during attempts
`to enter the 7-in. liner.
`
`Installation of the eighth isolation assembly was completed in a
`record time of 25.5 hours from the assembly makeup until the serv-
`ice packer was out of the hole.
`After installation of the final completion (Ng. 13), 11/2-in. coiled
`tubing was rigged up and the following runs were made.
`1. Ran in the hole to the top of the plug at Zone 6 and circulated
`clean.
`2. Ran in the hole with a pulling tool and retrieved the prong
`from the blanking plug.
`3. Ran in the hole with a pulling tool and attempted to retrieve
`the blanking plug. Pulled out of the hole without the plug.
`4. Ran in the hole and retrieved the plug.
`5. Ran the wash tool to TD and circulated clean.
`6. Ran the shifting tool for the sliding sleeve and began opening
`sleeves from the top down (Zone 8, 7, etc.). Unable to peas Zone 4.
`Pulled the shifting tool out and found it to be sheared.
`
`SPE Production Engineering, February 1992
`
`7 of 9
`
`67
`
`Ex. 2079
`IPR2016-01496
`
`

`

`RETRIEVABLE
`SERVICE
`PACKER
`
`SIDE MOUNTED
`GUNS WITH
`FIRING
`HEAD
`
`RETRIEVABLE
`COMPLETION
`PACKER
`
`LOCATOR
`TUBING
`SEAL
`ASSEMBLY
`
`BALL SEAT
`
`SLIDING SLEEVE
`
`Fig. 15—Parallel gun system.
`
`7. Ran a circulation nozzle to TD while circulating without any
`obstructions.
`8. Ran the sleeve-shifting tool with one extra shear pin installed.
`Observed increased drag forces from Zone 7 to 'ID, indicating some
`debris being pushed in front of the shifting tool. Shifted all sleeves
`from the bottom up (Zones 1, 2, etc.) with an observed overpull
`of 5,000 lbm at the surface to shift each sleeve. It was found that
`none of the sleeves was opened fully during the first opening run
`(Run 6). The sleeve-shifting tool came out unsheared, confirming
`that all sleeves had been opened.
`After eight coiled-tubing runs in 58 hours, the first well with the
`PSI system installed was ready to begin production.
`
`Performance of PSI System and Previous Systems. To compare
`the performance of the PSI system with that of previous systems,
`an actual completion/stimulation time analysis was constructed. The
`time spent for different operations is broken down into the follow-
`ing categories: Type 1—tripping time for successful trips; Type 2—
`stimulating time; Type 3—time spent as a result of equipment
`failures, including tripping time; Type 4—any type of waiting time;
`Type 5—other operations, such as packer setting, circulating, and
`curing losses; Type 6—final completion time; and Type 7—coiled-
`tubing operations. Figs. 14A and 14B show the time and fluid loss
`breakdown comparison for Wells MFB-15, MFB-13, and MFA-13.
`Additional time studies showed that the application of new
`methods reduced the average time spent per zone from 106 hours
`on Well MFB-15 and 78 hours on Well MFB-13 to 61 hours on
`Well MFA-13. Compared with Well MFB-13, use of the PSI sys-
`tem on Well MFA-13 reduced total completion time by 136 hours.
`Comparisons of the different types of operations show that time
`spent on tripping has increased as a result of the PSI system (130
`hours on Well MFB-13 and 177 hours on Well MFA-13). How-
`ever, a significant time saving on packer setting, circulation, and
`curing of losses has materialized. Time saving on equipment failure
`operations also materialized, despite the complicated nature of the
`PSI system.
`Use of the PSI system resulted in a significant brine saving from
`about 11,000 bbl on Wells MFB-15 and MFB-13 to about 3,300
`bbl on Well MFA-13. This is a direct saving of 7,700 bbl. Scaled
`for the number of zones, the saving is some 9,300 bbl of brine.
`At a cost of about $20 U.S./bbl, the total brine savings amounted
`to roughly $186,000.
`
`Conclusions
`During project evaluation, the perforating/stimulating time per zone
`was estimated to be 48 hours. When comparing this with the actu-
`al 61 hours spent per zone, one must conclude that the expected
`time saving did not materialize. However, the estimate of 48 hours
`was based on optimal performance; i.e., no allowance for equip-
`ment failures was made. If the actual time spent is corrected for
`equipment-failure-related time plus about 50% of the coiled-tubing
`
`68
`
`time (for plug retrieval), the time spent per zone comes to about
`43 hours, which compares well with the estimated time con-
`sumption.
`The brine consumption with the PSI system was estimated to be
`about 2,700 bbl for seven zones. The actual losses were 3,300 bbl;
`but for eight zones, which if scaled dotiin to seven zones comes
`to a consumption of 2,900 bbl. The estimated brine consumption
`was also based on optimal operation. The bulk of the actual con-
`sumption occurred during the time when Zone 6 was exposed to
`losses caused by a leak. Hence, it is considered that the estimated
`brine saving did materialize.
`The possibilities of restimulating selected zones individually and
`closing off zones producing at high water cut or GOR's are still
`to be tested; however, sliding sleeves have successfully been shift-
`ed in older wells in this field several years after installation. There-
`fore, we are confident that these options can be used when required
`later in the producing life of these wells.
`Further development of the PSI system is needed to achieve a
`one-trip system for sand operations. Sand erosion problems must
`be solved to increase tool life.
`Successful deployment of this horizontal-well completion system
`was the direct result of close collaboration between the operator
`and the service company. Both companies provided unique perspec-
`tives and complementary areas of expertise, which resulted in the
`development of this system in a very short period of time.
`
`1992 Updato
`Maersk Oil has successfully installed the PSI system in 14 horizontal
`wells since the field test of the system in the Dan Well MFA-13
`in 1989. In total, 126 zones have been completed with the PSI sys-
`tbm. The system has been deployed in conjunction with matrix-
`acidized, acid-fractured, and sand-propped fractured intervals.
`The average completion time per zone has been 85 hours, with
`a maximum of 110 hours and a minimum of 48 hours; hence, the
`originally estimated average time for completing a zone has never
`materialized. However, a significant saving in brine consumption
`has been achieved in all wells completed with the PSI system.
`The system has basically been used as originally designed, ex-
`cept for the retractable gun, which has never been field tested be-
`cause of erosional problems with the circulating sub and potential
`retrieval problems after firing and stimulating. The PSI system has
`consequently been run in two trips—one trip to perforate and a sec-
`ond to stimulate and isolate to complete matrix-acidized and sand-
`propped fractured intervals. This constraint in the current version
`of the PSI system has partially accounted for the additional com-
`pletion time spent in comparison with the initial estimates. A one-
`trip system, however, has been used in acid-fractured zones by use
`of a short 2%-in. TCP gun on the inner string extending out the
`end of the locator-tubing seal assembly.
`A parallel gun system (see Fig. 15) has also been developed to
`facilitate a one-trip system for sand operations. This system con-
`
`8 of 9
`
`Ex. 2079
`SPE Production Engineering, February 1992
`IPR2016-01496
`
`

`

`Authors
`
`Damgaard
`
`Murray
`
`Stout
`
`Rubbo
`
`Anders Darnmeard
`Is the manager of
`Drilling Services of
`Maria Energy Inc.
`In Houston. Since
`joining Mast* Off &
`Gash Copenhagen
`In 1981, he has held
`various drilling and
`nobelium positions
`for North Sea ac-
`tivitles. Damgaard
`holds a BS degree
`In electronics from the Danish Engineering Academy. Dan
`Banged is director of Technical Services for Baker 011 Tools
`In Houston. During his 16-year tenure there, he has held posi-
`tions In research, U.S. and International operation

This document is available on Docket Alarm but you must sign up to view it.


Or .

Accessing this document will incur an additional charge of $.

After purchase, you can access this document again without charge.

Accept $ Charge
throbber

Still Working On It

This document is taking longer than usual to download. This can happen if we need to contact the court directly to obtain the document and their servers are running slowly.

Give it another minute or two to complete, and then try the refresh button.

throbber

A few More Minutes ... Still Working

It can take up to 5 minutes for us to download a document if the court servers are running slowly.

Thank you for your continued patience.

This document could not be displayed.

We could not find this document within its docket. Please go back to the docket page and check the link. If that does not work, go back to the docket and refresh it to pull the newest information.

Your account does not support viewing this document.

You need a Paid Account to view this document. Click here to change your account type.

Your account does not support viewing this document.

Set your membership status to view this document.

With a Docket Alarm membership, you'll get a whole lot more, including:

  • Up-to-date information for this case.
  • Email alerts whenever there is an update.
  • Full text search for other cases.
  • Get email alerts whenever a new case matches your search.

Become a Member

One Moment Please

The filing “” is large (MB) and is being downloaded.

Please refresh this page in a few minutes to see if the filing has been downloaded. The filing will also be emailed to you when the download completes.

Your document is on its way!

If you do not receive the document in five minutes, contact support at support@docketalarm.com.

Sealed Document

We are unable to display this document, it may be under a court ordered seal.

If you have proper credentials to access the file, you may proceed directly to the court's system using your government issued username and password.


Access Government Site

We are redirecting you
to a mobile optimized page.





Document Unreadable or Corrupt

Refresh this Document
Go to the Docket

We are unable to display this document.

Refresh this Document
Go to the Docket